THE AMERICAN SOCIETY OF MECHANICAL ENGINEERS 345 E. 47th St, New York, N.Y. 10017 97-GI-61 The Society shall not be responsible for statements or opinions advanced in papers or cfiicussion at meetings of the Society or of its Divisions or Sections, or printed in its publications. Discussion' is printed only if the paper is published in an ASME Journal. Authorization to photocopy material for Internal. or personal use under circumstance not fang within the fair useTprovisions. of the Copyright Act is granted by ASME to libraries and other users registered with the Copyright Clearance Center (CCC) Transactional Reporting Service provided that the base fee of 50.30 per page is paid directly to the CCC, 27 Congress Street. Salem MA 01970. Requests for special perrniesicin or bulk reproduction should be addressed . to the ASME Technical Pubfishing Department. All Rights Reserved Copyright 1997 by ASME . Printed in U.S.A FIELD-EXPERIENCE ON DLN TYPHOON INDUSTRIAL GAS TURBINE MARCUS H. H. SCHOLZ SIMON M. DEPIETRO European Gas Turbines Ltd. Lincoln, United Kingdom ABSTRACT The second Generation of EGT's G30 DLE combustion system was introduced after a successful series of high pressure rig and engine tests. This paper covers how operational problems with field commissioning hardware on the lead DLN machine were dealt with, leading to achievement of reliable low NOx hardware. Several changes were applied to the early design which improved the mixing and reduced the effects of high temperature distortion and combustor dynamics. This resulted in increased life of the burner and changed the characteristics of dynamics. It also led to very low emission levels with an outstanding capability for turndown of CO with NOx below 25 ppmvd (15% 02) over the whole load range. Further coverage is given to the effect of field tuning, and of fuel composition on the amplitudes and frequencies of dynamics. The installation has been supported by on-line condition monitoring of engine parameters, emission levels and ambient conditions, which are also discussed. The general overview of site history is followed by a summary of lessons learnt in field comparison to development test bed. NOMENCLATURE CEM CO LBO FSNL Continuous Emission Monitor Carbon Monoxide Lean Blow Out Full Speed No Load NOx ppmvd TOp ITT RMS UHC LCV Tgas SG cDRZ Oxides of Nitrogen (NO+NO2) Parts per million by volume, dry gas Turbine Operating Temperature (PTexit temperature-Inlet temperature) • constant Turbine Entry Temperature Route Mean Square Unburnt Hydrocarbons Lower Calorific Value Temperature of gas fuel in K Specific Gravity Reaction zone equivalence ratio INTRODUCTION The first industrial gas turbine with Dry Low NOx (DLN) technology from EGT was supplied and commissioned in March 95 after an accelerated rig and engine development programme. The 4.5 MW Typhoon Gen-set forms part of a Combined Heat and Power (CHP) plant at the Arnhem headquarters of the Dutch chemical company Akio-Nobel. The site provides an ideal engine location for endurance testing and evaluation, where the operation is essentially baseload with excess electrical output sold to the grid. Three combustor build changes over a period of 13 months from the initial installation with NOx levels of 55 ppmvd in Phase IA, resulted in hardware producing less than 15 ppmvd with virtually no CO and no UHC at baseload conditions. (Table I.) TABLE 1: Milestones in EGT's DLE Programme Date (Commission) Phase 3. March 95 IA Oct. 95 IB May 96 2A Hardware modifications Dynamics level Single point Design, 3 cusp radial inward pilot ignitor centre position IM Design, revised piston Seal, cooled centre ignitor, high dynamics damper 2M Design, profiled pre-chamber off-centre ignitor, reduced film cooling Flow matched components 27.6 kPafRMS 150 Hz 10.3 kPa/RMS 150 Hz 0.7 kPafRMS 360 Hz Emissions NOx 55 ppmvd 37 ppmvd Problems fretting, carbon deposit Tip temperature, mixing parts life, Tip temperature Pre-chamber, distortion load shed operation <15 ppmvd Presented at the International Gas Turbine & Aeroengine Congress & Exhibition Orlando, Florida — June 2–June 5, 1997 Downloaded From: http://proceedings.asmedigitalcollection.asme.org/ on 12/29/2014 Terms of Use: http://asme.org/terms engine performance data and a CEM system. This equipment was accessible on-line through a direct modem connection for condition monitoring. The combustor itself has experienced over 10000 running hours and the life time prediction is at least 25000 hours or 10000 cycles. As part of EGT's G30 technology programme, the 030 DLN combustor has been specifically developed for EGT's small Gas Turbines up to 8 MW. It is based on a simple fixed burner geometry, using a part premixed, lean-burn approach and has been described in detail by Norster and DePietro (1996). The combustor (Figure I.) consists of a radial inflow swirler, swirler-slot injection and a premix chamber. A pilot burner is situated in the centre, but has a flush face with the radial swirler slots and is mainly used for ignition and to stabilise the flame on part load INTRODUCTORY HARDWARE The initial phase IA hardware was unable to meet the Dutch legislative limit of 37 ppmvd NOx, (15% 02) [actually 65g/G/ heat input]. The hardware was installed firstly to provide a means of commissioning the boiler and generator and secondly to gain some field experience with DLN in commercial duty. The immediate problems encountered on site started by reestablishing the ignition window which had moved since the endurance run on the test beds in Lincoln. After starting the unit and achieving Full Speed No Load (FSNL), the synchronisation and the loading of the generator proved to be more straight forward than experienced on the development test beds. NOx was measured at 55 ppmvd (15%02), using both the CEM and a portable analyser. This was consistent with the levels measured in Lincoln. Internal combustion pressure oscillations (dynamics) were measured at levels of 27.6 kPa/RMS above 90% load, using piezoelectric transducers fined to the burner ignitor ports and pressure casing. The most significant issues arising from the introduction of this hardware related to ignitor life and carbon formation on the recessed ignitor at low loads. The severity of this carbon build up was such that after 4 hours the ignitor recess would be effectively closed off, thereby isolating the ignitor from the gas mix (Figure 3). Subsequently after the engine was shut down, re-ignition was not possible. Sustained running at full load on the other hand resulted in overtemperature of the central pilot zone, leading to oxidisation of the pilot and overtemperature of the ignitor tips. conditions. Figure 1. Burner Assembly This design can be retrofitted to all Typhoon gas only engines, since it does not require changes to the present centre casing arrangement. (Figure 2.) Figure 3. Oxidised and carboned Pilot Tip Figure 2. Centre Casing Arrangement In addition to ignitor and pilot tip temperature problems high load operation highlighted another major issue not seen in development testing. After one week running at full load, high levels of low frequency dynamics (nominally 27.6 ld'a @ 150Hz) caused The site installation has been supported with an extensive data acquisition system, which comprises of combustion parameters, 2 Downloaded From: http://proceedings.asmedigitalcollection.asme.org/ on 12/29/2014 Terms of Use: http://asme.org/terms severe fretting at the transition duct combustor liner sealing joint. The transition duct and piston ring sealing arrangement though wear coated were found to have grooves up to 2mm deep in places (Fig.4.). As a consequence, the unit was limited to 3.4 MW to minimise damage and the risk of material ingestion into the turbine. burner was modulated to balance the tip temperatures, the exhaust temperature spread, but more importantly the dynamics. Fuel tuning option enabled the dynamics to be reduced to less than 10.3 kPa on all burners. Combustion inspections completed at 800, 1200 and 5000 hours indicated the hardware was in good conditiontwith no re-occurrence of fretting. Problems which were apparent though were tip temperature drift with time and poor ignition after compressor cold wash. Three pilot burners had to be exchanged after they developed a progressive tip temperature drift characteristic with time but this was achieved during inspection to minimise machine downtime. Fuel Split Schafule ......... —Main Figure 4. Transition Duct damaged through fretting EMISSION COMPUANT HARDWARE The problems experienced with the previous set of hardware led to an improvement programme targeting both the high dynamics levels and the levels of NOx in order to meet the emission specification. The continuing development programme in Lincoln in parallel with the field commissioning had already produced some very encouraging test-rig results with single digit NOx figures. Phase 1B hardware was introduced based on these developments. New features of the Phase 113 include an improved mixing main burner with multi-point injection hardware, a central air cooled pilot tip design featuring an air-swept ignitor. Dynamics were reduced by improving the flame stabilisation on the pilot and by damping the lateral pressure waves in the combustor liner. An improved seal arrangement was also introduced to minimise leakage airflow between transition duct and combustor and thereby control NOx. This revised hardware was introduced in October 1995 and the unit re-commissioned. The light-up characteristics remained unchanged, however, the main/pilot fuel split schedule defined on the test bed could not be applied to the site installation. Load swings of up to 0.5 Mw were experienced at 85% load and very high tip temperatures (transiently 1200 Deg C) were seen at 95% load. The fuel split schedule which regulates the ratio of fuel being injected through the main and pilot is dependent upon load and controlled as a function of the engine operating temperature (T0p). A typical fuel schedule is shown in Figure 5. It became apparent, that the translation of the hardware from UK to Dutch Natural Gas was an issue that needed serious consideration. By exhaustive fuel split mapping a schedule was established that permitted safe and stable operation across the load range. NOx emissions levels were recorded at 37 ppmvd (15%02) by the CEM at ISO conditions and the Dutch emission acceptance test certified compliance with the permit. The installation of fuel tuning valves in the main burner pipes enabled gas flow to be tuned manually to each burner. By selective setting of these valves, the total gas flow to each 200 250 300 350 450 400 Opeatim Porn, TOp 500 550 we&c3 Figure 5. Fuel split schedule Both the tip temperature and ignition problems were caused by the cold wash sequence, where dirt, fouling the compressor was flushed through to the combustor and more importantly into the pilot tip cooling air feeds. These feeds were very small (taking less than 1% of total combustor air flow) and had a disproportionate effect on burner performance by affecting the stoichiometry at the ignitor tip. This degradation was observed through the online engine healthmonitoring data link which allowed sufficient time for intervention and the prevention of potential damage. LOW NOx HARDWARE After 5225 hours of operation with IB hardware, the final phase 2 hardware was installed in June 1996. It consisted of the exchange of the main burner and pilot assembly with a further improved mixing through a multi-multi main burner design, designated 2M to signify 2 side wall injection holes. It also featured an offset ignitor pilot design without tip cooling with a bluff front face to aid flame stabilisation. The stoichiometry of the combustor reaction zone was richened by an increased effective area transition duct to account for the improvements in mixedness but the combustor barrel was not replaced. Again there was no change in operational characteristics at lightup, but at baseload the combustor proved to be operating very close . to LBO limits. The baseload pilot percentage with Dutch gas 3 Downloaded From: http://proceedings.asmedigitalcollection.asme.org/ on 12/29/2014 Terms of Use: http://asme.org/terms gases dewpoints tend to be relatively consistent (CO Deg C) the Wobbe Number can vary significantly: e.g. from Dutch Gas at 37 MlThm3 to Alaskan Gas at 48 MJ/Nm3. Conventional burners are designed to operate within given bounds of pressure ratio (typically 1.03 to 1.4), and the design rules for this are well understood, however, adopting and following rules becomes all the more important for a DLN combustor. All the G30 development testing (both rig and engine) was completed on UK Pipeline Quality Natural Gas in the facility in Lincoln. Early field experience was obtained from the lead machine in Holland running on Dutch Groningen gas which includes 14% Nitrogen as a diluent. Table 2 illustrates the difference for these gases in both theoretical parameters of calculated flame temperature, fuel penetration (into premixer slot), and measured parameters of NOx and main burner pressure drop. (I4%Nitrogen) had to be set at a higher level to compensate for the mixedness effects with the new burner compared with values typical of UK gas. The dynamics level after modifying the baseload pilot split were still measured at less than 0.7 kPa at all load points. The pilot tip temperatures were less than 700 °C and NOx at these higher pilot flows was measured at 14 ppmvd (15%02), CO was measured below 2 ppmvd. (Figure 6.) Both emissions and tip temperatures have remained stable at commissioning values and no re-occurrence of ignition problems has materialised since the simplified design has no air passages to accumulate water or dirt FIELD COMMISSIONING EXPERIENCE The introduction of the G30 DLN system into the field has been supported and controlled to a large extent by the engineers directly involved in the development of the combustion system. This has meant that lessons learnt in the field i.e. operational difficulties and the results of hours associated with site machines have been fed directly back into the development programme. Some of these lessons and observations are discussed below: Effect on light up (ignition) window A combustor ' light up window' is defined as the pilot/main fuel ratio and gas flow required to give ignition. During development testing it had been found that to achieve consistent DLN burner ignition lean or ' soft' lights were required i.e. with very low gas flows and relatively small pilot %' s. Overfuelling to create a rich or ' hard' light simply resulted in no ignition due to the creation of an over rich zone around the ignitor tip. Translating this into the Figure 6. 14 ppmvd NOx vs ambient variation over 24 hours CEM Emission vs. Ambient 25 BO 6tco 0 70 OatizipaNd:$5000,9:55-afb.calsoacc- 00 OS% CO co dacCa%35 0141°61MISI3Sta) o - 20 60- NO* CO ppnwc11. RM.] 0 e Ocernko 50 COppm a NOx(corr) 44+ ORH% 002% xParnb +Tomb +44. 414,440++ - .4444++++.0.444444-44.4. 4.44et4le+4++ +444.44+14.4. +++++ 4+ +4.4. + 4444+141. 20 awaeafrocardandoroaattOna 5 attootararetWagtiana ag eirartabreetwogemprocaveterAw 10 0 83 8 E 0 0 0 0 8 0 a si s 0 7r. Cl 0 0 0 0 C. o 0 el el 4: cri ° 8 ,e. 0 0 .74 el 24 hour log experience on Dutch gas showed that attempting to increase the throttle angle to give the same heat input as on UK gas was unproductive. The effect of the increased gas volume was to swamp the ignitor and prevent a flammable air/fuel mixture reaching the ignitor plasma. The results showed that the critical parameter was the pilot gas volume at ignition not the heat input and that this could be Gas Composition and Temperature ' Natural Gas ' covers a broad range of possible compositions depending on both, the type of gas field and the age of the well. Even removing the direct from the ground "well gases" and analysing what are termed " Pipeline Quality Natural Gases " leaves considerable variation in composition and Wobbe Number. Although on these 4 Downloaded From: http://proceedings.asmedigitalcollection.asme.org/ on 12/29/2014 Terms of Use: http://asme.org/terms • temperature and better mixing were in practice offset by the need to operate at a significant higher pilot percentage to minimise the lean chug dynaniics and maintain stability. In comparison to the Pipeline Quality Natural gases a typical oil field "well gas" may include a significant proportion of higher hydrocarbons and therefore has a relatively high Wobbe Number. The lower burner pressure drops associated with that fuel gases mean that fuel system feedback and coupling with combustor dynamics would be a real possibility. In reality however, the dewpoint of these gases tend to be at higher temperatures (i.e.+20 to +40 °G), that it would not be handled without fuel heating, the effect, which is to increase the gas volumetric flow rate and thus the burner pressure ratio. achieved by balancing both overall fuel flow and pilot/main fuel split. Typical ignition fuel splits range from 18 - 25% pilot. Effect on Flame Temperatures Theoretical flame temperatures for the respective gases are shown in Table 2 and would suggest that since thermal NOx is temperature dependent a reduction in NOx should be measurable between field and development results. This predicted difference was not seen in practice on any sites or on any of the hardware standards and did not appear to be dependent on absolute NOx levels (whether 55 or 14 ppmvd N0x). The observations and conclusions drawn was, that because of the nature of the premixer, other factors such as burner pressure ratio were far more important to NOx levels than the flame temperature. FFT Analyser Trace 1000 TABLE 2: Gas Fuel Effect 900 Properties North Sea Gas BOO Groningen Gas 700 •-• Wobbe Index 47.18 37.25 j 600— .E 400 psdil/m3 1 Flame Temperature [°K] SOD 1798.8 1783.4 300 . @ ORE=0. 53 NOx (156/002,dry) 203 15 (4) 14 (8) 103 [ppmv] 0 0 (a) (pilot %) 50 100 150 19$ 245 295 345 385 435 485 535 585 Frequency (112] Main burner AP [psi] 19.47 31 Figure 7. Pm-mix characteristic @ 360 Hz @ 6% pilot FIT Analyser Trace Effect on fuel system pressure ratio (burner pressure drops1 1080 900 Initially, no hardware modifications were included to adapt the burner to the higher gas volume flow rates of the Dutch Groningen Gas. The result was an increase in burner pressure drop (illustrated in Table 2 for the Phase 2 hardware). Because of the passage injection system design of the 630, this higher pressure drop translates into an increased jet penetration into the slot. The result of this was seen in the field as the inability to run as low a pilot split as achieved on the test bed in Lincoln i.e. the design stoichiometry of the reactor was too lean to permit operation at this level of premix. This exhibited itself on the machine as a pronounced LBO dynamic characteristic (or lean chug). On LIK gas a very low pilot could be sustained at baseload without loss of flame or significant chug. A characteristic pre-mix tone is shown in Figure 7., correctly tuned for stoichiometty, a medium amplitude pilot driven peak (160 Hz) and the dominant hot tone premix dynamic peak (360 Hz). Whilst Figure 8. shows a typical chug tone at 60 Hz, for a combustor approaching LBO limit. As mentioned previously, there was no NOx-advantage measurable on the Dutch gas. The benefits of lower theoretical flame 800 700 IL 600 503 .E 400 303 203 100 0 50 80 130 180 no 2110 330 380 410 430 530 510 Fitqutney [Hz] Figure 8. Lean Blow Out! Chug tone @ 60 Hz Based on the site experience to date and experience of variable gas composition a set of design rules have been established for 5 Downloaded From: http://proceedings.asmedigitalcollection.asme.org/ on 12/29/2014 Terms of Use: http://asme.org/terms burner pressure drop and burner hole size for the 030 system. These rules utilise a dewpoint temperature corrected Wobbe number. Whilst these valves proved of considerable value in early development testing, the experience on both the production test bed and in the field has shown little need or benefit from fuel tuning. The optimisation of burner pressure ratio's and improved manufacture control of effective areas in Phase 2 hardware effectively making tuning valves unnecessary. Wobbelndex = LCV 18 IrS— G Tgos Further site evaluation and validation will form an essential part of establishing the upper and lower limits of the design rules. Ignition System One of the major concerns raised during the 030 concept discussion was the utilisation of a no cross light tube and only one ignitor per combustor philosophy i.e. no redundancy in ignition capability. The concern was that if any one of the six ignitors, ignitor leads or ignitor channels in the multiplexed energiser box developed a fault the unit could not be started. However, after 10000 hours on the lead machine, and with another 13 machines in duty no problems have arisen from the ignition system reliability. The lesson being that provided the ignitors are kept cool either by air cooling (as Phase 1B) or gas cooling (Phase 2) and kept free of carbon plugging there will be no major issues on combustor ignition. In addition the phase 2 hardware with offset ignitor also eliminates the effects of cold wash being retained in the ignitor cooling passages. As discussed previously it is the pilot gas volume flow rate that defines the ignition window. With increased numbers of machines entering duty some variability in the position of the light up window (pilot % and light up gas flow) has been seen. This is a function of manufacture tolerance on combus-tor/bumer effective area and fuel splitter valve and is the inevitable result of making six independent ignition and combustion zones. What has also become evident though is that, provided the ignition window is adequately mapped during commissioning and the % pilot and light-up flows set at mid range values, ignition can be guaranteed. Fuel tuning In Phase 1B and Phase 2, the main burner feeds were fitted with fuel tuning valves. In the case of the 1B these were commercially available diaphragm valves illustrated in Figure 9. whilst those fitted to Phase 2 were purpose designed and made for DLN fuel tuning. Tuning Valve Ambient temperature effects Variation in ambient temperature was found to have a significant effect on the level of 68Hz-chug dynamics at baseload. This is an effect also seen with high Wobbe Number sites (i.e. low gas volumetric flow rate). The ambient temperature effect only became apparent on introduction of the Phase 2 design where the level of premix was significantly better. The mechanism for this effect is that as ambient temperature rises so the compressor discharge temperature rises, and in order to maintain the turbine exhaust temperature (and thus the design TET) the fuel must be reduced. This results in a lower temperature rise and hence leaner combustor operating point. What this means to the combustor is, that the hotter the ambient temperature, the leaner the reactor stoichiometry and the closer the combustor operates to the LBO limit. In order to counter this, an ambient biased fuel schedule was devised in which the baseload fuel split is modulated as a function of the inlet temperature above 15 °C. By altering the reactor mixedness the margin before LBO is improved and chug dynamics are reduced. Figure 9. Alao Unit Combustion Inspection Using these valves each of the 6 main feeds could be selectively tuned enabling the total gas flow to each combustor to be modulated. By iterative tuning it was possible to reduce the burner dynamics that might arise as a result of burner or combustor effective area variability. 6 Downloaded From: http://proceedings.asmedigitalcollection.asme.org/ on 12/29/2014 Terms of Use: http://asme.org/terms required to achieve reliable load shed capability for machines tuned to higher levels of premix and single digit NOx. Operability and load handling One of the positive benefits found on moving to the field installation was that of speed stability. In the Lincoln test bay where engine load was provided by a water dynamometer, shaft speed stability was not good (particularly at simulated no load conditions. Speed variations of +/- 200 rpm were typical at the nominal shaft speed of 17250 rpm. Concern was raised that this variation would not allow synchronisation with the grid, however, the first run with a generator indicated that there was no issue on speed fluctuation. No speed synchronisation problems have been encountered on any site and it was evident that this was a brake problem unrelated to combustor or control stability. Loading and unloading proved to be uneventful and again significantly better on generator than on water brake with regard to speed stability. The major handling problem proved to be that of rapid unload or load shed. This is an issue for all DLN systems operating with a lean premix flame but is particularly an issue for small machines in generator drive applications. The most arduous unload scenario is a Grid Breaker open load shed from full or baseload to no load. This has to be achieved without loss of flame and this test forms part of the requirement at a number of the Field sites. The mechanism for load shed from baseload to FSNL (for a single shaft machine) is as follows. The Grid breaker opens and there is an almost instant loss of load on the turbine. Since the throttle valve for gas flow is fully open and the turbine is no longer frequency (and hence speed) locked to the Grid the turbine speed starts to increase. In order to prevent turbine overspeed the throttle is closed rapidly to a sub FSNL condition (i.e. to the Governor Blow Out limit) and then re-opens once speed rise is contained and the turbine is restored to its FSNL condition and is ready to resynchronise. The 030 combustor weak extinction limits with greater than 10% pilot far exceeds the capabilities of the conventional combustor, however, in order to achieve NOx levels below 15 ppmvd, low pilot flows are required and this inevitably compromises the flame stability. At these pilot flows and with the high level of main burner pre-mixing, load sheds can only be achieved by rapid increase of the pilot fuel flow. Preliminary issues during site testing related to the controls recognition of combustor flameout. The temperature monitor routines in the software which utilise information from the exhaust temperature thermocouples were initially set up for conventional combustor exhaust spreads and required modification to operate with the more uniform DLN exhaust spread. During testing it was also evident that the response time of the turbine exhaust thermocouples and thus the ability of the control system to advise a revised fuel split requirement was too slow. A fuel split override logic was introduced to the software, such that once above a pre-determined load point defined by a TOp set point the pilot splitter valve would be stepped open from a very low flow setting to nominally 25% open value when a load shed detected signal was received from the throttle governor. This proved to be very effective for current standard of machines tuned at 15 to 25 ppmvd NOx (15% 02) but the indications are, that further work is EMISSION CORRELATIONS There have been theoretical investigations into the effect of humidity, ambient pressure and temperature on lean premix combustors for a number of years. Some authors (Lewis 1981, Visser and Bahlmann 1994) could relate the impact of fuel flow control due to ambient variation correctly. In fact, their theoretical studies suggested that the humidity effect of the EPA correction could be omitted and that the temperature effect would be opposite to the effect encountered with conventional diffusion flames. The control of the single shaft Gas Turbine is based on maintaining a constant Turbine Entry Temperature (TET) at baseload. This is implied from a derived Turbine operating temperature or TOp as discussed previously, consequently a combined effect of ambient air condition and fuel flow will regulate the flame temperature at the same value. Determining an ambient temperature effect on NOx and CO has been one of the major goals of the CEM and continuous performance monitoring exercise to enable modifications to EGT's emission correction formula. From data collected throughout the installation Phases, EGT derived conclusions, which imply a logarithmic relation between the change in ambient temperature and the produced NOx. With regards to the level of mixing it was apparent, that the 2M burner was less sensitive to ambient effects than the IM design (Table 3.) TABLE 3: Sensitivity to ambient Temperature Hardware ANClx/5, T1 1M ( 37 ppmvd) 0.7 ppmvd / PC 2M (<I5 ppmvd ) 0.15 PP""d/ °C This follows the general tendency, that Nthc formation becomes less sensitive to ambient variations as premixing is approached. REFERENCES Norster, E.R. and DePiefto, S.M., 1996, Dry Low Emissions Combustion System for EGT Small Gas Turbines, Institution of Diesel and Gas Turbine Engineers. Norster, E.R. and DePietro, S.M. et al, 1996, Development of a Dry Low NOx Combustion System for the EGT Typhoon, PowerGen 1996. Kowlcabi, M. et al, 1997, The Development of a Dry Low NOx Combustion System for EGT Typhoon, to be presented at ASME 97 Visser, B.M and Bahlmann, F.C., 1994, Variation in the NOx emission of Gas Turbines, ASME 94-GT-261 Alkabie, H.S. and Norster, E.R, 1994, ISO-Correction Formula for G30-NOx Emission, EGT Internal report. Lewis,0.D,1981, Prediction of NOx Emissions,ASME81-GTI19. 7 Downloaded From: http://proceedings.asmedigitalcollection.asme.org/ on 12/29/2014 Terms of Use: http://asme.org/terms
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