Operational Strategies to Control Energy Bills OWEA Plant Operations Workshop May 22, 2014

Operational Strategies to
Control Energy Bills
OWEA Plant Operations Workshop
May 22, 2014
Kevin Krejny
My Goals of Presentation
• Give real numbers, problems, solutions from Ohio
WRF. In regards to energy costs
• Understand your energy costs and needs
• Operational Strategies to lower energy costs
• Touch on energy purchasing strategies
• Show how to track that you are getting better
• Show that with any style or size plant, there are
energy savings available
Western Regional WRF
Montgomery County Water Reclamation (since 2008)
• Flow- Avg. 14.94 MGD
Median 13.81 MGD
• 12.25 MGD Summer
15.59 MGD Winter
20.0 MG Design
• TSS Loadings – Avg. 22,559 lbs Median 19,939 lbs
• 22,141 lbs summer
•
22,960 lbs winter
55,000 lbs Design
Ammonia Loadings – 1800 lbs per day
• cBOD Loadings – Avg. 24,628 lbs
• 24,651 summer
Median 23,583 lbs
24,605 lbs winter
38,400 lbs Design
• We have lots of concrete, what technology is in the
concrete is old, inefficient, and creates constant
headaches. But we have started to fix that.
Other Facilities
• Fairborn WRF – 4.5 years
• Clark County SW Regional WRF – 2.5 years
• Greene County – 1 year
o
o
o
o
Beavercreek WRF
Sugarcreek WRF
Cedarville WRF
Clifton WRF
kWh
WRF Energy usage
(keep in simple)
• Aeration
o Activated Sludge
o Digestion
• Pumping
o Influent
o Internal plant elevation
o RAS/WAS
• Other
o Lighting
• Indoor
• Outdoor
o HVAC
o Dewatering
o Ultraviolet Disinfection
Aeration
• 40-60% of total usage depending on plant type
o Activated Sludge/Aerobic Digestion - up to 60%
o Trickling Filter (pumping needs)/Anaerobic - less than 20%
o Many combinations
• Activated Sludge
o Ammonia and cBOD removal
o Lower MLSS could mean less aeration (tanks) needed
o Look at ammonia effluent
• If <0.25 mg/l, likely over aerating
• Know your permit limits, no or high winter ammonia, can turn back
• Aerobic Digestion
o If going landfill – weigh aeration energy costs vs. VS destruction
o Once pass 503 reg parameter (i.e. SOUR test), turn back air
o DO >2/0 mg/l can turn back aeration
Jet Aeration vs.
Fine Bubble Diffusers
Fine Bubble Diffusers
Increased Efficiency
Jet Aeration Tanks
MLSS
Average
3206
lbs solids in Instanteous average
aeration
Flow
cfm
89127
16.2
3048
Fine Bubble Tanks
30 min
Settle
ammonia
(mg/l)
SVI
Average
cfm
30 min
Settle
ammonia
(mg/l)
281
2.65
88
2026
270
1.70
% less
33.5%
3.9%
36.0%
Last year side by side comparison
Western Regional WRF
700 HP Huffman Multistage Centrifugal Blowers
Newer technologies 10-15% more efficient
aeration kWh per lb cBOD
1/1/08 to present
2.50
1,400,000
1,300,000
2.00
1,200,000
1,100,000
1.50
1,000,000
900,000
1.00
800,000
700,000
0.50
600,000
0.00
500,000
aeration kWh per lb cBOD
influent cBOD lbs
Linear ( aeration kWh per lb cBOD)
Linear (influent cBOD lbs)
Pumping
• Proper sized pumps
o Likely oversized to meet peak demand that might only occur 5% of year
o Great to have various sized pumps and use combinations
o Use wet well height to help keep pumps in the proper area of pump curve
• Variable Speed Frequency Drives (VFD)
o Replace old VFD’s
o 10 years old, might not be doing what they were designed to do
o Help to keep pump running in sweet spot of curve
• High/premium efficiency motors
o More hours on motor, more payback with switching over
• Clean/replace Air Relief Valves (Next slide)
• Track MG pumped/kWh used
o
o
o
o
Great if pumping station separate from rest of plant
Only true way to measure if your changes are working
Cannot use $$$, because this cost changes yearly
A kWh is always a kWh + a MG pumped is always a MG pumped
1,300
1,200
Variable Frequency Drive and Air Relief Valve
Improvements Made in Early 2013
kwh/MG Pumped at Pre-Treatment (2008-13)
1,100
1,000
Avg 802 kwh/MG
900
Avg 695 kwh/MG
800
700
600
13.3% Reduction
500
AVR replaced 1/1/13
VFDs Installed 2/1/13
400
kwh/MGD (PTP)
after ARV
Linear (kwh/MGD (PTP))
Linear (after ARV)
Return Activated Sludge (RAS)
• Turn down you RAS rates
o
o
o
o
o
o
o
o
o
It is the pounds of RAS returned, not the flow
7,500 mg/l @ 2 MGD = 10,000 mg/l @1.5 MGD = 15,000 mg/l @ 1.0 MGD
Benefit of increase detention time in aeration basins
Promotes Biological Nutrient Reduction (BNR)
Less Nitrate coming back around
Reduces RAS pump usage
WAS is thicker going to digester
Reduce supernate efforts
Less volume needed for digestion – could prevent the need for more
concrete
HVAC
• Know your staffing and building needs
• DO NOT heat/cool building to 70 degrees that
people enter only once a day
• Use windows/doors to self regulate air flow and
temperature needs
• Never run a heater in a blower room
• Buildings below ground rarely need Heat/AC,
maybe ventilation
• Moving water will not freeze in a building
• Natural gas cheaper than electric heat, right now
• Electronics like cold not heat
Lighting
• Use motion detection to turn on/off lighting
• Outside lighting
o
o
o
o
Should evaluate how much is needed (know where people work)
Is plant staffed 24/7 or not
Light sensors to turn on/off daily
You do not need to play football at a WRF
• Replace old lights with LED
Make sure they get enough hours of use
Do not need LED on a light that is used once a day for a plant check
Replace aging/high use lights first with LED
The more hours a light is on, the more savings you get and faster pay back
in a LED lighting upgrade
o Adding savings of longer life, less time replacing bulbs
o
o
o
o
FACT
• It does not matter how you are
billed for electricity, moving
electrical usage off peak and
keeping a steady load profile
all day and year will save you
money.
Energy billing options
• Tariff pricing
o What energy supplier in your area has written in numerous tariffs
o Changes several times a year, hard to follow and confirm being billed
properly
• Fixed Pricing
o One set cost per a period of time
o Usually 1-2-3 years
o All inclusive
• Index Pricing
o
o
o
o
Energy price changes hourly
Based on regional demand and usage
Can be very good at certain times
Can keep you up at night at other times
•What do they all
have in common?
Answer
• They all have a Historical Peak Demand component
specific to your facility in the bill
• This can be great it you control and predict your
peaks
o Peaks are set at the five highest hours, on different days, from the previous
year
o Usually set during afternoon of 90 degree plus days in July or August
o 2013 were all from one week in July
PEAK LOAD (MW)
PJM RTO
DATE
HOUR ENDING
7/18/2013
17 (5pm)
157,509
7/19/2013
15 (3pm)
156,077
7/17/2013
17 (5pm)
154,044
7/16/2013
17 (5pm)
151,421
7/15/2013
18 (6pm)
150,315
Delivery Year:
2009-10
$ 102.04
First Energy $ 102.04
DPL/Duke/AEP
2010-11
$ 182.85
$ 182.85
2011-12
$ 116.15
$ 108.89
2012-13
$ 16.74
$ 20.46
2013-14
$ 28.37
$ 28.37
2014-15
$ 128.17
$ 128.17
2015-16
$ 134.62
$ 342.30
2016-17
$59.37
$114.23
SO WHAT Can you do
• Turn off or back as many treatment processes as
you can for a couple hours during these days
o Minimal treatment for three hours will not effect your 24 hour composite
sample that much
o Fill wet wells and turn off digester aeration
o Stop dewatering
o Stop RAS/WAS, can get caught up later by increasing rates
o Turn your aeration back as much as possible
o Remember during these 5 hottest days, you are likely to have your lowest
flows of the entire year
o If you have newer emission friendly generators you can run them to
completely get off the grid
o RICE NESHAP started 5/3/2014 reduces options to control these charges
Running Plant generator (12 times)
hit all 5 peak hours
Money saved (7/147/15)
Money spent/ results
•
•
•
Fuel = (4800 gal * $3.50)
= $16,800
Labor = (12 days*3
hr*$35/hr*1.145 OPERS)
= $1,442
$18,242 Spent – no DPL
bill during time ($12,
560)
•Cost of $5,682
•
•
•
Doing nothing
Capacity Charge
$89,404
We spent $5,682 to go
off the grid
Capacity Charge for
(7/14 7/15) = $5,611
• Total Savings =
$78,111
Great Online tool
• Updated regional usage every 5 minutes
https://edatamobile.pjm.com/eDataWireless/SessionManager?a=instLoad
Block and Index Pricing
• Takes the certainty of Fixed Pricing (Block) and
allows a portion of your usage to be on hourly index
pricing
Block and Index
• Can combine several accounts for the block
• Mixture of drinking water pumping and wastewater treatment
help keep a flat profile of accounts
• Lowest Block amount is 1 MW a month or 720,000 kWh per
month
• Can block of 1 MW intervals
• Can do this at anytime or amount (pricing changes daily)
• Suggest, if large enough, hire a energy broker to make these
transaction and lead you through
• If you can control energy needs through facilities for short
periods of time, you can save a lot of money
• Get to a flat load profile – Energy suppliers love knowing they
have clients with consistent loads = cheaper pricing
Questions or Corrections
• Now
or
• Later
[email protected]